We’re having some trouble with a T100 motor. Testing with a multimeter has suggested that there’s a break in one of the wires. The white wire is showing as having infinite resistance between the it and the other wires. The resistance between the blue and green wires is fine - very low. We’ve tested it with known working ESCs, so the problem isn’t there.
Do you have any idea how we might go about fixing this without compromising the waterproofing? We don’t even know where the break is, nor how to find it.
CAUV (Cambridge Autonomous Underwater Vehicle)